So, it turns out I'm mildly retarded.
I've been fighting huge vacuum leaks this week. I replace the upper plenum and runner gaskets. Improvement, but still hear some pretty bad hissing. Turns out I didn't put O-rings on the driver side injectors. Derp.
Once I got that fix, bam. Vacuum leaks gone. Car starts. No hissing. Got it re-timed, and then it starts missing badly. Timing light shows that the poor thing is losing spark. Quick look at Megatunix, and I only have 10.8 volts coming out of the battery. An HEI module doesn't work very well below 12 volts. Turns out I left the pin I used to hold the brushes in the alternator down when I took it apart a few weeks ago. No brush contact with the stator = non functioning alternator.
Pulled the pin, put the battery on the charger. Going to give it an hour to juice back up and see where we are.
Saturday, November 24, 2007
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